January-inside work only for
next three months. Two pairs of hanging knees constructed for cabin from
American oak- bolted into existing frames where possible or else external
planking with large screws. Chain plates –3pairs made from stainless steel 60mm x 8mm flat. Difficult to
assess correct angle for attachment of bottle screws. Much help from
Dave Clout & Al.- full use of their
facilities-makes light work of difficult material. Excellent idea from Dave –using sliding
wedges to hold upper section of chain plate tight between beam shelf &
sheer plank thereby minimising lateral movement on vertical pull from rigging.
Mark started on cabin interior- starboard seating –first attempt- too high –not
good for my short legs! Useful visit to Boat Show with Pam- £700 spent on
electronics. – cheap compared to Vic –he will be
spending a fortune to kit out his new boat. Horrible wet W/E – last metal floor
bracket- securing forward dead wood –preventing lateral movement of mast foot.
The heads compartment is nearly complete.

February –work started in cabin- first the starboard
side: L shaped settee berth
and nav. station.The
bench seat is finally located at 14.5” above the floor which with 3” foam
cushion should the correct height. The back rest is set into the frames and the
top panel completes the panelling –based on a hard wood frame. Really quite difficult to get right due to all the curves.
The plywood –supposedly –mahogany faced Far Eastern ½” WBP supplied by Watford Timber really is very
poor quality. I wish I had rejected the second load as well !
16/17th
–spring weather is here but will it last? Excellant
progress- nav. table in situ and settee berth nearly
complete. Heads compartment primed –plumbing needs completion. Morale good!
Roof of work shop made watertight by Graham and far end cleared out in
preparation for storage of
23/24th-
the portacabin roof still leaks badly. Port side-
galley work started. Work top set at 30”. Flavel
cooker TOO large (and it really is not that big) due to tight turn on bilges!
Oh dear- replacement triple burner hob/grill to be
purchased instead and “oven tin” in place of proper oven to be investigated.
Does anyone need a good second hand cooker-going cheap –only £100?

March – the “cool box” won’t fit either under
the worktop but at least I can install a decent sink unit without any problems
otherwise the galley is coming along fine. The new
April- cabin roof strips with beading pattern
added, all sanded down (what a mess!) and treated with Dek
Oljs –looking quite nice. Meanwhile skylights are
nearly complete-except for safety glass and protective stainless rails.
Starboard coving line tackled with great reluctance- very difficult to achieve
a smooth line using router held against 3” wooden batten- lots of errors
requiring filling with plastic wood but finished result acceptable. The rubbing
strip can wait awhile! Cockpit floor panels edged in U shaped rubber channel
(£45 cost!) –glued on with Bostic. Teak
cockpit floor kit now being assembled. Teak grab
rails for coach roof fitted by Mark-excellent job. Faulty wrought iron keel bolts
drifted out and temporarily replaced by 21mm studding – 4 removed without
difficulty but number 2 seriously stuck and wedged in by excessive use of
undersized drift and 28lb sledge hammer . Total doom & gloom - how could I
do this? Rescue plan (to extract bolt) formulated by Peter Parry & Dave
Clout –thank God for friends? Sky lights now being treated
with Dek Oljs 2 –coming
along fine. Promising new contact in Maldon who will
make the new keel bolts in mild steel.
May – Two attempts to extract bolt by means drawing
it out from bottom of keel with extractor failed due to metal fatigue. Bolt cut
in half at ballast/keelson interface by means of keyhole surgery with 14”
industrial hacksaw blade. Finally top section drilled out by Dave Clout- using
1 ¾” drill size. Lots of drama –morse
end snapped but success eventually with second drill bit. Very
hard work (for him and drill!)
Skylight installed –looks good but rain drips in. Large boxy sliding
coach roof on low parallel runners built- looks horrible –back to drawing
board. Mk2 version built from cutting down Mk1 –sloping
runners with low sliding hatch. Just too narrow but looks much better.
Spars arrived on May15th –look fine. Gaff saddle missing. Mast
lifted into shed for 4 coats of two pack varnish. Rigging order with Cindy
Parker cancelled –my patience has finally run out- Classic Marine very helpful
in advising on replacement order. Superb book arrived- Hand,Reef & Steer by Cunliffe-
a really useful addition to my reading list! Tom –barman at the
June- Jubilee W/E- Mark on holiday- final fitting
for sliding coach roof- many hours spent
on “squaring up “ inboard end of bowsprit to fit teak locating blocks. Prepare
and fit oak dowel tapering from 2” to 1” x 14” long to fill “drilled out” cavity in keelson for
keel bolt no:2. Unusually straight forward. This will need re-drilling to size (1”) when
keel fitted on Wed. Long overdue tidy up in shed-even the hoover
seemed tired afterwards. Ballast keel re-sited wrong way round by Hiab (driver is obviously not a sailer). 2” moat built round top of keel and filled
with large quantity of “black pudding” (tar based gunge).
The legs are reattached to frame to get extra clearance Hull successfully
relocated on to ballast keel and new keel bolts (3-6 only) refitted-all in
pouring rain! At least it looks like a
boat again albeit rather high in the sky. Keel bolt holes 1 & 2 drilled
through and bolts fitted. The seatings for heads of
keel bolts are
excellent –lots of black pudding used and nuts tightened repeatedly –lots of gunge oozing from keel interface –most satisfactory!
Finally crane returns again–legs detached and boat re-sited at ground level
again (not exactly level ) and mast stepped –all in ONE hour of frantic effort
by Peter Parry ,myself and reluctant crane driver. Raining as
usual. Rush home for Dac-Doc session
(emergency on call)
from 7-11pm Off to Oban next day at 5am- why do I feel tired?
Successful
week sailing in Western Isles –pretty eventful but refreshing- back early (too much
wind & rain)- now for the standing rigging- supplied by Moray from Classic
Marine. Stalocks (clever little devices for attaching
lower ends of wire rope shrouds to rigging screws) to keep me beat for one day then it is
full speed ahead. Mark back at work - great to have him around again. Lots of
varnishing work on remaining spars. First
attempt at scaling mast a resounding failure. Boom winched up on deck
–all 32ft and
located into gooseneck fitting- it REALLY is long! Bowsprit fitted after many
trials. Held up by stem head and crane iron fittings –I do wish Dave C. would
work a little faster.
July-life is now more interesting but also
more scary! My first trip to the mast head will remain a memorable experience –poor Mark can’t bear
to look up whilst winching –Graham Halden has now
taken over-and I feel a great deal happier.
Running rigging set up –first jib &
foresail then gaff- peak & throat halyards finally twin topping lifts –
200metres of 12mm rope consumed! Wooden blocks pickled in D1 for 7 days. 3”
blocks changed to 4” –former too small. Very exciting and
satisfying. Fife rails fitted –essential for halyards –now 8 in number.
Thank goodness my luck has changed. Extendable dolphin striker and mainsheet
horse needed for completion. Weather very hot- Sandy (younger son) great help
up mast.

August-mainsheet horse returned for shortening by 5”
–Dave C. “not amused”. Finally installed along with 45m.
of 14mm rope –now I need some cleats. Boom
crutch made from 1” S/S
side tubes and BZ mahogany strut-elegant and useful for
supporting boom. Lots of small rigging jobs inc. running back stays
finally completed. Very fetching brass cowl vents purchased for fitting on dorade boxes in front of cabin roof –most satisfying
(unfortunately they do not actually vent the heads or
wet locker as intended but they look great anyway)

September- long awaited visit from
Cindy Parker (Wilkinson Sails). Jib luff too
long due to upward angulation of bowsprit –to be
lowered. Likewise foresail luff wrong- inner forestay
set incorrectly at hounds –should be crane iron level. Mainsail (VAST!) needs
extra eyes but otherwise OK (relief). Long hot but very
enjoyable day. The long wait was worth it. Now for re-jigging the
rigging and a second sail fit next month. The boat does feel close to coming
alive. Lots more varnish being applied to toe rails and rubbing strip.
Disaster- forehatch
accidently
dropped on my fingers- two finger tips fractured –lots of blood & pain++
: trip to A & E on Sunday – more grief but back to work on boat by midweek
–not too bad really! Deck drains
connected under deck to drains under counter stern –water collected into water
butt for future use. Cleats & fairleads fitted to stern -trial & error
as usual. Winches mounted on BZ mah. Blocks –offset
hemispherical- layered and turned on lathe. Quite labour intensive. Glued and
screwed to deck & cockpit sides walls.
October-weather still holding good-
varnishing coming on well. Stern deck vent arrived (at LONG last) from Vetus- look smart. Companion way doors- slatted in braz. mah- fitted with difficulty.
Deck draining working well- water butt full after a few hours
of light rain. 14 hessian sacks now arrived
for the “take up” procedure. Sandy back up the mast –new inner fore stay fitted
and other rigging arrangements completed. Winches seated on mahogany bases
–very smart! Work well –excellent purchase for bosun
chair lift . Now it’s raining again +++ Very miserable
indeed. Time to fit the bilge pump assembly. Pump
expired after 15minutes- not a good omen! Cockpit floor needs sealing (once
& for all)- new sealing strip required after
building up floor rim.
December-many hours of hard work
cleaning and sealing the bilges, followed by coats of primer and red bilge
paint. Tidying up the cabin has started in earnest. Time
to rediscover the engine and complete fuel connections. Rear cabin
bulkhead and lids for access hatches completed. Cabin/ heads door installed 1”
thick- should act as “watertight” door in case of severe flooding! Some obstruction to passage way but acceptable. Useful time
spent on Xmas & Boxing Day doing odd jobs- nasty head cold – pretty
miserable time (if all said & done!) New Year’s Eve- engine started using
internal cooling circuit only –total disaster when external cooling
circuit added (using header tank)– “dead engine” and external circuit water
draining from inlet manifold. What have I done to my new engine? At
least the Xmas photo looks

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